Small update on the old blue dinosaur...
Since stepping down from the 750 Ultra carb in my experiment with running a more conservative 'baby' 650 Street HP, I'd introduced a wicked stumble right off idle - which has been annoying me for the past 9 months (but I'd learnt how to live with it). But I don't like band-aids, much prefer solutions...
I was suspicious that the new PCV valve I'd also installed might be to blame (it was just some generic later model type PCV, certainly not designed for low vacuum old Chevs) - so I removed it and bingo - the flat spot was gone and the car feels a million dollars to drive - crisp and smooth everywhere.
We put it back onto the dyno at Goody's Garage to reset the idle mixtures (managed to refine them a bit more which was good), and then it was time for another experiment...
I reported previously that the 14" x 3" Ryco air filter was robbing 10rwkW and this bugged me. So I decided to do 3 tests:
Baseline from last time on dyno - best run with no air filter was 229.5rwkW.
Now with the PCV removed:
1. Ryco air-filter (red line) - 231rwkW. Observations: erratic behaviour down low (seen in both power and torque curves), air:fuel went 11.8, 11.9, 12.0, 12.1, 12.2, 12.3, 12.2, 12.1
2. No air-filter (blue line) - 234rwkW. Observations: air:fuel went 12.1, 12.2, 12.1, 12.0
3. K&N air-filter (still 14" x 3") (green line) - 237.1rwkW. Observations: both power and torque lines super smooth. Air:fuel went 12.5, 12.4 - near dead flat.
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And that final test was actually the 7th consecutive pull, so things would've been getting hot. I still find it funny that it performs better with the K&N over no filter at all. And I'm certainly not chasing power, but it's always awesome to see a nice little increase like that.
For interests sake, my idle vacuum has now also progressed from 4.5" with the old 750 Ultra, to 6" with the 650 Street HP, and now to 7" with the removal of the PCV valve. The manners, drive-ability, crispness and smoothness are finally the best I've ever experienced with this engine.
On that note: this engine has now clocked up it's 10 year anniversary. I got Eric to do a leakdown test for housekeeping. He reckons the results shocked him (super consistent and quite incredible for an engine like this after a decade) - best was 7%, with the majority at 8% and one at 9%. Handy reference and I hope to now go another 10+ years, touch wood!
Check out the Mustang - a mates new car - you could eat your dinner off this thing...
Bring on the Summer cruising - I hope we're allowed out soon!
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